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Ukko Kari

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Everything posted by Ukko Kari

  1. What is a good horn in your experience? For a common 90h x 45v horn of 12 inches width and 6 inch height, the vertical polar pattern will widen below 3.7khz, exceeding 90 degrees at just below 2khz, according to this article: https://www.prosoundtraining.com/2010/05/24/understanding-horn-directivity-control/ Even the 18 Sound XT1464 is 'small'. Used with other elements in a vertical 'array' of 3 elements [MTM] leads to increased directivity in the vertical dimension, even when the pattern control is falling from the horn.
  2. One way to cure diffraction is to flush mount the cabinets in a baffle wall with a layer of absorption, like 1" thick. Realistically, larger radius corners should have been used on my boxes, but 1 1/4" is getting a bit hairy to handle in a hand held router even with a large add on baseplate, and 1 1/2 is about the limit without going to MDF substrate and using machined corners. http://www.tapeease.com/cabinet1.htm I could have gone the skeletal route with multiple layers of thin plywood instead, ending up with curved sides, large radius on the baffle. Did I mention the dust was *incredible* when routing all of the corners to 1 1/4" radius? Doing this outdoors with a slight wind, it was still problematic, it was like it was snowing wood dust out.
  3. At the end of the day, you have to ask yourself is the juice worth the squeeze? Additional amplifier channels, more complexity, an additional surface for diffraction from your main woofer.
  4. Perhaps juggling chainsaws would be easier than picking trade-offs. Baffle width, roundover size, cabinet depth, height, volume, adequate port area, bracing, ability to get cordless drill inside enclosure for installing the pocket screws on the last side... portability, ease of assembly, etc.
  5. Mic 1/4" from top woofer dust cap: Edit: I don't recall if eq and crossover were enabled, it's been a while since this was measured. Might have to disable the DSP and re-measure this.
  6. I had hoped that the tuning would shift up enough by shortening the ports 2 inches, but their proximity to the side walls and floor of the enclosure means that they are acting like they are much longer than they physically are. It is a bit of a pain to finesse the port length, but I would like to get the tuning point up just a wee bit higher. I can live if they aren't 40 hz.
  7. I also checked for excursion minima with sine waves at high levels. With the shorter ports, excursion minima was 34-34.5 hz. We can debate minutia all day long, but that doesn't change much. When the voice coils have some heat in them, the impedance will shift as well.
  8. As an experiment ( per Lilmike ), I hooked up a pair of UCA-202's, output on one, and measure on the second to get rid of the cross talk issues. Apparently, the absolute value for impedance is off, but the <20hz cross talk is gone.
  9. Had a bit of time today to pull the lower woofer, wiggle the ports out of the baffle, shorten to 8" long, installed they are 8 3/8" total. Net interior volume went up by 0.11 cu ft, to a total of 9.63 cu ft. I had not saved the impedance .mdat prior, but looking at the screen shot, the upper impedance peak fell a small amount, as it would when the box volume increased. Removing 2 inches on each port only raised the tuning ~ 1 hz, observed excursion minima was at 34-34.5 hz. I also found a leak around a screw during testing, the foam seal had compressed some since assembly.
  10. The closest I could place the cursor was -0.9 degrees, yes it coincides with the peak on the right, but the others are shifted some. I get 0.5 degrees at 0.7 hz above the left peak, and centered it's already at 20 degrees.
  11. Here's a screen shot with the phase:
  12. Based on your post, I would have to say no, since the 0 crossing would be around 24 hz, based on the phase reported in REW.
  13. Again, same measurement of the co-axial through the autoformer, however this time with only -6 db attenuation.
  14. And now for the interested, the same measurement as above through a model 3636 autotransformer at maximum attenuation, -12db.
  15. BMS co-axial through passive network:
  16. Pair of woofers in parallel, approximately 20 feet of 14awg speakon cable into the box: ( didn't account for that in Rleads box of REW) Note, port length unchanged, 33hz excursion mimima +/- 1/2 hz observed. Will be shortening ports to bring the tuning up when I get time to do some more measurements.
  17. Built Lilmike's impedance jig and took a few measurements. Raw 15PR400 hooked up with short 2 foot leads:
  18. Coming soon ( in the next month or so, busy with work and life ) impedance measurements, thanks to Lilmike.
  19. The real answer is it depends. I agree that it may only be a small fraction of a difference. It would be interesting to note the input power to the amplifier to see if the efficiency / breaker utilization changes any, which may be a bigger deal for large systems with racks and racks of amplifiers running off a generator, or in a venue where power is subject to droop. ( older wiring, smaller services )
  20. I have found the ports are acting like they are almost the full depth of the cabinet. I started the generator in REW at 25 hz, then raised the volume level until excursion was a few mm, then in 1 hz increments raised the frequency, checking for excursion minima, which ended up at 33 hz, +/- 1/2 hz. I had a feeling that tuning would be lower than expected, from the proximity of the ports to the enclosure side walls, and each other. Having calculated the volume of the bracing, and ports a few times, using the manufacturers supplied volume on the woofers, along with a good estimate of the horn displacement along with the compression driver, I can confidently say the internal volume of the enclosure is 9.52 ft^3. +/- a small percentage. Dual 7 5/8" ports, 10" long should have put tuning at 40 hz in 9.52 ft^3. When I have a chance, maybe next weekend, I will pull both and shorten them to 8" to try and note the result.
  21. I read that article many years ago, and in some cases, it can be applicable. Keep in mind that you are also driving essentially a dummy resistor load, and the results may be different driving a reactive load, where back EMF is reflected on the power supply.
  22. I wish it was 65F.... tonight the forecast is close to -20C... [ -4F ] No outside measurements for a while here.
  23. These will be primarily for HT, however I may want to use them outdoors at times in 1/4 space. With the lightweight drivers, they aren't that bad to move.
  24. No, I have not measured impedance yet, when I can get to it, I will.
  25. One cabinet has been assembled at the moment. Yes, at the moment working on measurement, waiting for nice warm weather both to measure outdoors, also to order Duratex when the risk of freezing has passed. I am not against a series connection, it would increase the applied voltage and cut wire losses, increasing damping factor. A warm voice coil increases in Re, and if my math is correct, at just 50C, the VC Re would increase to 3.724 ohms.
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